The Grim Reaper!

Kish2604

Administrator
Staff member
Next on the list to be done is a leaky oil filter housing and a new set of plugs. The current ones have done a fair bit of duty and are due for replacement. Getting the OFH out also seems to be a half day job as the intake manifold must come off to access a lone bolt hidden under it. While I am in there I have a small to do list of things to check for piece of mind. I will update soon again.





Sent on the move from my S7edge
 

Kish2604

Administrator
Staff member
Update, Spent a long over due day with my car this past Sunday, had a long list of items to get through, Oil filter housing gaskets needed to be changed, since the manifold was coming off I took the opportunity to clean the Intake ports as a diy, new spark plugs (NGK 5992) and swopped the HPFP with another to troubleshoot something I saw in the jb4 logs,

The Oil filter housing was tackled first by stripping the cowls, air snorkel and DCI’s, 2 water pipes and the oil cooler pipes removed, ER CP and Throttle body fully removed next, then loosening the manifold bolts and nuts and try to unclip this annoying junction box under the manifold. Once that was done proceed to remove the manifold, be careful with any ancillary wiring and piping that might catch the manifold as you remove it. Then it was the turn of the E-torx bolts around the housing and the one poorly positioned under the manifold area. Once that’s out the OFH just lifts out.

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That was placed into a container to drip the oil out before going to soak and wash in degreaser. The OFH is 2 parts bolted together and then mounted onto the side of the block. Wash, clean and prepare all the surfaces for new gaskets before mating. Once the OFH was closed up and torqued to spec the attention turned to the intake manifold. It has on it a little nipple that’s used as a boost reference for the DV/BOV and is probably 3mm in diameter and made of thin plastic. This nipple has a bad habit of breaking of after getting brittle, it is also the cause of turbo flutter when used in more than stock boost applications.

I am using an ER charge pipe with a TIAL Bov and TIAL recommend using a minimum ¼ inch diameter line to keep the bov responding fast enough and not creating any surge. So the tiny reference was ground of with a Dremel tool then a 4mm pilot hole tapped into the manifold, this was followed up by an 8mm bit to widen it. A 1/8npt tap was then used to cut threads into the hard plastic manifold. Once the brass fitting could screw in and out fully a little bit of Pratley quickset was mixed onto the threads and the fitting screwed in tightly. Because of the NPT thread pitch from the tap and the fitting, the brass fitting went in tight and was dressed with the remainder Pratley around the base. This was left to dry.

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Next up was the intake ports and boy was it dirty. 100k km of use and it can build up quite a bit of gunk. Keep in mind I don’t have the same tools that Carbon doctor has to do this so I had to rely on some good old fashioned elbow grease and ingenuity. As my luck would have it the car had 5 of the 6 cylinders closed. I tested this with a bit of carb cleaner into each port and they all held tight. My tools for the task was a Dremel with extendable goose neck, some brass wire heads in different shapes, some dental tools including a few types of picks mirrors, a compressor and with blower tool. A can of carb cleaner and lots of rags. Two hour later the first 5 cylinders were completed, the motor was turned over till cylinder 5 sealed tight and the last one was finished. NB. while the end product is nowhere near the Carbon Doctor finish; it was good enough from what it originally looked like till I get an opportunity to get it walnut blasted properly.

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The manifold was closed and sealed while the 6 plugs came out for the first start up, this is so any dirt that may have gotten into the cylinder (99% chance nothing didn’t) would have a place to exit out the plug holes. Once done A new set of NGK 5992 iridium plugs were gapped and sent to do duty in the respective positions. The charge pipe and ancillary’s were closed up and a liberal dose of engine degreaser was applied to the engine bay for it wash.

The car was left to idle for about 15 mins after being washed and taken out for a drive and a log or 2 after. All in all a lengthy days work but all so worth it.

Thanks for looking!
 

Kish2604

Administrator
Staff member
So a couple of updates since my last post on this thread, after doing the Oil filter housing gasket and washing the oil out I thought i was in the clear with regards to the front end of the motor, couple nights later i went out to grab some logs and the serpentine belt gave up the ghost... trust me its scary when your at triple digit speeds and the steering just goes heavy without any warning or sound. :thumbdo: thankfully i wasn't to far from home and after a quick inspection i got it home safely to deal with the next day,

what i didn't realise is that the Oil filter housing was dripping oil directly onto the belt and tensioner over a period of time, i guess the degreaser to wash it up was the last straw for it to finally throw in the towel. Since i didn't want to open this area up again i figured i would sort it all out once and for all. Ordered and replaced the 2 deflection pulleys as well as a new belt, the tensioner looks to have been replaced while under motorplan so i left that alone. Pulleys were inspected for chips or damage the front was bolted up.

While my hands were dirty and the front jacked up i took the opportunity and pulled the front wheels of to fit the brake bushes i got from Axis. These bushes replace the rubber/plastic ones that come fitted from the factory that some engineer thought would be great for a reducing NVH, but they definitely aren't worth it a few years later when they wear and allow the caliper to flex as it squeezes onto the disc during hard braking.

the fitment process isn't difficult,using a thin flat screwdriver you can pry the rubber ones out. Remove the C clips on the new bushes and slid it in with some copper-slip for lubrication. I had 2 of them be a little stubborn so a quick clean with a dremel and a wire brush to remove the stubborn dirt along with gentle tapping with a hammer and an extension (if you going to use anything to tap these bushes in please insert the guide pin inside it first and use a suitable sized socket to tap on the outer rim of the bush so it doesn't flare the edge) and it slotted perfectly into position.

Lubricate the guide pins with more anti seize copper slip and your good to go. closed the both sides up and immediately the pedal felt a lot better from the reduced flex in the moving parts. What i also noticed since then was a circular heat band that developed on the disc from the caliper clamping incorrectly has slowly worn away over the last week or two, some really hard braking exercises have also revealed its a mod definitely worth its weight in gold if you value consistent pedal feel and response. Well done Axis on a great in house developed product!

product link: Here

:clapper:

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Kish2604

Administrator
Staff member
So this sunday the 29th a few of us decided to make the trip to the track and chase some times, being the first time at the track with the car all sorts of thoughts start running through your head, so with a little prayer i lined her up and crossed the finish line 11.9 seconds later with an exit of 199kmh... needless to say i was ecstatic!... the day remained pretty consistent with 3 of my 5 runs at 11.9seconds, 1 @ 12.1seconds and 1 at 14seconds were the car bogged down on the line and i just cruised down the strip...

results thread Here
 

Kish2604

Administrator
Staff member
Thanks guys...

@Yasheen... its the only gap I get... anyways nicer to be typing a report back than actually being outside working on something...
 

Twinz

Forum - Support
Staff member
Excellent thread with useful updates. Once again well done with the track times :clapper:

How has the new bushes changed the drive & braking? Any NVH issues?
 

moranor@axis

///Member
Official Advertiser
Thanks for the Review Kish I will be making up that tool I spoke of to make fitment even easier on the guide bushings :rollsmile:
 
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